ログイン
言語:

WEKO3

  • トップ
  • ランキング
To
lat lon distance
To

Field does not validate



インデックスリンク

インデックスツリー

メールアドレスを入力してください。

WEKO

One fine body…

WEKO

One fine body…

アイテム

  1. B. 理工学域; 数物科学類・物質化学類・機械工学類・フロンティア工学類・電子情報通信学類・地球社会基盤学類・生命理工学類
  2. b 20. 紀要
  3. 金沢大学工学部紀要
  4. Vol.18 No.1

Strain Characteristics of Underground Model Pipe During Incomplete Liquefaction

https://doi.org/10.24517/00065283
https://doi.org/10.24517/00065283
8411ff8f-40ab-4d63-a92c-aed7e2b2d4c4
名前 / ファイル ライセンス アクション
AN00044309-18-1-35-41.pdf AN00044309-18-1-35-41.pdf (260.1 kB)
license.icon
Item type 紀要論文 / Departmental Bulletin Paper(1)
公開日 2022-01-27
タイトル
タイトル Strain Characteristics of Underground Model Pipe During Incomplete Liquefaction
言語
言語 eng
資源タイプ
資源タイプ識別子 http://purl.org/coar/resource_type/c_6501
資源タイプ departmental bulletin paper
ID登録
ID登録 10.24517/00065283
ID登録タイプ JaLC
著者 Kitaura, Masaru

× Kitaura, Masaru

WEKO 92299
e-Rad 70026269

Kitaura, Masaru

Search repository
Miyajima, Masakatsu

× Miyajima, Masakatsu

WEKO 69332
e-Rad 70143881
金沢大学研究者情報 70143881
研究者番号 70143881

Miyajima, Masakatsu

Search repository
著者別表示 北浦, 勝

× 北浦, 勝

WEKO 9906
e-Rad 70026269
研究者番号 70026269

北浦, 勝

Search repository
宮島, 昌克

× 宮島, 昌克

WEKO 28
e-Rad 70143881
金沢大学研究者情報 70143881
研究者番号 70143881

宮島, 昌克

Search repository
書誌情報 金沢大学工学部紀要
en : Memoirs of the Faculty of Technology Kanazawa University

巻 18, 号 1, p. 35-41, 発行日 1985-03-20
ISSN
収録物識別子タイプ ISSN
収録物識別子 0022-832X
NCID
収録物識別子タイプ NCID
収録物識別子 AN00044309
出版者
出版者 金沢大学工学部
出版者(別名)
出版者 Faculty of Technology Kanazawa University
抄録
内容記述タイプ Abstract
内容記述 This paper describes the dynamic behavior of buried pipeline during incomplete liquefaction. Buried pipeline systems have been damaged extensively by soil liquefaction. The procedures of mitigating the damage due to soil liquefaction were recently proposed. The extent that the buried pipe are not damaged should be made clear in advance in case of ground improvement as countermeasures to liquefaction. Therefore it is important to understand the behavior of the buried pipeline during incomplete liquefaction.
Experiments were performed employing the pipe whose two ends were free. The pipe was buried in loose, saturated sand stratum. The model sand stratum was vibrated by a transient harmonic wave with a frequency of 5 Hz. The experimental results showed that the dynamic strains took the maximum value as the ratio of excess pore water pressure was between 0.5 and 0.75. This was explained in terms of resonance of the system consisting of the buried pipe and model ground. Furthermore the effects of the buoyancy on the buried pipe and structure during incomplete liquefaction were discussed.
著者版フラグ
出版タイプ VoR
出版タイプResource http://purl.org/coar/version/c_970fb48d4fbd8a85
戻る
0
views
See details
Views

Versions

Ver.1 2023-07-27 09:11:26.321887
Show All versions

Share

Mendeley Twitter Facebook Print Addthis

Cite as

エクスポート

OAI-PMH
  • OAI-PMH JPCOAR 2.0
  • OAI-PMH JPCOAR 1.0
  • OAI-PMH DublinCore
  • OAI-PMH DDI
Other Formats
  • JSON
  • BIBTEX

Confirm


Powered by WEKO3


Powered by WEKO3